Session 2 - 01 (Energy Efficiency Potential Assessment of Chandrapura TPS, DVC)
Session 2 - 01 (Energy Efficiency Potential Assessment of Chandrapura TPS, DVC)
Session 2 - 01 (Energy Efficiency Potential Assessment of Chandrapura TPS, DVC)
Om Prakash
SDE (Mech.) & Energy Manager,
CTPS
DVC TPP at a Glance
Station Capacity Commissioning
Thermal power plant
U-III July 68
CTPS 630 MW (1 X 130 MW + 2 X 250 MW) U-VII Nov 11
U-VIII Jul 11
Total 7090 MW
Chandrapura Thermal Power Station
Damodar Valley Corporation
Total Capacity – 630 MW
Unit Size – 1 X 130 MW and 2 X 250 MW
Date of
Unit Boiler / Turbine
Unit Capacity (MW) commissioning
No. make
(year)
Overview
individual components
component groups
sub-systems
complete systems
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Components available for mapping
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Absolute
Deviation 0.0 3.0 2.1 5.3 5.16 5.8
(A-B)/A %
Gap Identification and Analysis
Boiler
The coal fineness of coal mill AB through 50,100 & 200
mesh was less than 75 %, an indication of poor performance
of coal mill, resulting in the higher UBC in ash (fly ash and
bottom ash was in the range of 1.03 % and 5.58 %
respectively) and lower boiler efficiency.
O2 % at APH inlet was measured in the range of design
value, whereas at the outlet it was measured 6.5 % against
the design value of 5.0 %, an indication of APH seal leakage
and poor performance of APH.
Main steam pressure at turbine inlet was maintained at
143.0 kg/cm2 against the design value of 149.0 kg/cm2,
resulting in higher operating turbine heat rate.
Soot blowers were under commissioning stage.
Operating Boiler Efficiency – Un burnt Carbon
Gap Identification and Analysis
Condenser
Condenser back pressure was higher in the range
of 0.14 Kg/cm2(a) against the design value of
0.1033 kg/cm2(a), resulting in higher TTD & higher
operating turbine heat rate.
Condenser Performance
CW Temp Condenser
CONDENSER TTD
Rise Back Pr.
Effectiveness
Units K 0C Kg/cm2(a) %
Operating Condition
Design Condition
Gap Identification and Analysis
Heaters
Feed water temperature gain in the HPH 6 was
around 100C less than that of design value, resulting
in higher TTD & higher operating turbine heat rate.
H P Heaters Performance
HPH 6 HPH 5
Design Condition
HPH 6
HPH 5
L P Heaters Performance
TTD (K)
LPH 1 LPH 2
LPH 1 LPH 2
Gap Identification and Analysis
Turbine
The HPT, IPT & LPT cylinder efficiency was close to
that of design efficiency.
HPT, IPT & LPT Cylinder Efficiency
Design IPT
HPT Operating
LPT
Heat Rate Deviation amongst Controllable
Parameters
Absolute
Reference Actual Δ Heat Rate
Parameters Unit Deviation
(A) (B) (kcal/kWh)
(A-B)
Main steam temp oC 537 535 2 1.3
Main steam Press kg/cm2 149 143 6 7.8
Hot Reheat Temp oC 537 535 2 1.2
SH Spray t/h 0 8.7 0 0.0
RH Spray t/h 0 0 0 0.0
Condenser Press mmHg(abs) 76 103 27 54.5
Feed Water temp oC 246 236.7 9.3 7.7
DM Makeup % 0 2.1 2.1 15.5
UBC in B/A % 1.5 5.58 4.08 12.2
UBC in F/A % 0.5 1.03 0.53 5.3
Exit Gas Temp oC 140 143.8 3.8 4.6
(Corrected)
Excess Air % 19.5 19.4 0.1 -0.7
HPT Efficiency % 88 87.6 0.4 1.9
IPT Efficiency % 92 91.5 0.5 1.9
-ve gain in Kcal/Kwh, +ve loss in Kcal/kwh
Assessment of Energy Efficiency Potential
(Short Term) – At a Glance
Short Term Potential in terms of TOE
Assumption PLF 85%,
Oil GCV 10000 kcal/kg
Operati HR Deviation TOE per
Potential Parameters for Improvement Reference
ng (kcal/kWh) year
Main steam temperature(0C) 537 535 1.3 242.00
Hot reheat temperature (0C) 537 535 1.2 223.38
Un burnt in bottom ash (%) 1.5 5.58 12.2 2271.03
Un burnt in fly ash (%) 0.5 1.03 5.3 986.60
DM Make up (%) 1.0 2.10 8.1 1507.82
Total 5230.82
Short Term Potential in terms of TOE
2271.03
1507.82
986.60
242.00 223.38
1451.97 3685.77
930.75
achieved (TOE/year)/
Heat rate (Kcal/Kwh)
Implemented During
Actual reduction in
(Rs.Lakhs approx.)
implementation
Expenditure for
Total savings
Rs. In Lakhs.
Parameter
Sl.
Action Taken
No.
*Assuming coal cost 2000 Rs/t for GCV of 3500Kcal/kg , PLF 84%, Oil GCV 10000 kcal/kg
Implementation and Monitoring
implementation (Rs.Lakhs
rate (Kcal/Kwh)
Expenditure for
Parameter
approx.)
Sl.
Action Taken
No.
*Assuming coal cost 2000 Rs/t for GCV of 3500Kcal/kg , PLF 84%, Oil GCV 10000 kcal/kg
Implementation and Monitoring
(TOE/year)/ Rs. In
Actual reduction
implementation
Expenditure for
Implemented
Total savings
in Heat rate
(Kcal/Kwh)
Parameter
achieved
(Rs.Lakhs
approx.)
During
Lakhs.
Sl.
Action Taken
No.
AOH
3 detection test. 40.0 52.80
(579.7)
• Arrested passing steam line drain
valve to condenser.
• Cleaning and rectification of
Cooling Tower (drift eliminator
cleaning, V-bar and nozzle
replacement in cooling tower).
*Assuming coal cost 2000 Rs/t for GCV of 3500Kcal/kg , PLF 84%, Oil GCV 10000 kcal/kg
Implementation and Monitoring
achieved (TOE/year)/
Heat rate (Kcal/Kwh)
Implemented During
Actual reduction in
(Rs.Lakhs approx.)
implementation
Expenditure for
Total savings
Rs. In Lakhs.
Parameter
Sl.
Action Taken
No.
*Assuming coal cost 2000 Rs/t for GCV of 3500Kcal/kg , PLF 84%, Oil GCV 10000 kcal/kg
Implementation and Monitoring
(Rs.Lakhs approx.)
(TOE/year)/ Rs. In
Actual reduction
implementation
Expenditure for
Implemented
Total savings
in Heat rate
(Kcal/Kwh)
Parameter
achieved
Sl.
During
Lakhs.
No. Action Taken
`
*Assuming coal cost 2000 Rs/t for GCV of 3500Kcal/kg , PLF 84%, Oil GCV 10000 kcal/kg
Implementation and Monitoring
Actual reduction in
(Rs.Lakhs approx.)
(TOE/year)/ Rs. In
implementation
Expenditure for
Implemented
Total savings
(Kcal/Kwh)
Parameter
achieved
Heat rate
During
Lakhs.
Sl.
Action Taken
No.
6 10.0 8.0
alignment/adjustment . (85.0)
• Alignment of APH
rotor.
• Arrest Air infiltration in
boiler.
*Assuming coal cost 2000 Rs/t for GCV of 3500Kcal/kg , PLF 84%, Oil GCV 10000 kcal/kg
Operating Model (Post AOH)
Overall Achievements
Before After
Sl. %
Item Unit Design Impleme Implem
No. Improvement
ntation entation
Turbine heat
1 kcal/kWh 1954.2 2013.1 1965.1 2.38
rate
Boiler
2 % 86.62 84.76 86.17 1.66
efficiency
Gross heat
3 kcal/kWh 2256.4 2375 2280.5 3.98
rate
Unit
4 % 38.15 36.18 37.62 3.98
efficiency
Specific coal
5 kg/kWh 0.55 0.678 0.65 4.13
consumption
Overall Achievements
Savings after
Sl. No. Item Unit Implementation
of EE Measures
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